Of 152 Handley Page Hastings constructed, only two aircraft crashed/ditched into the sea, with no loss of
life and no serious injuries. One aircraft a C-1 TG579 of 48 Squadron RAF Changi came to grief just off RAF Gan in the Maldives
in 1960, this is well documented on other pages on this site. There appears to be very little known regarding the other Hastings
a C-1 TG613 from 99 Squadron Madras Presidency Squadron from RAF Lyneham which met its end in the Mediterranean on 22nd July
1953 in somewhat dramatic style, making the TG579 episode look like a picnic in comparison!
TG613 had previously taken off from Lyneham en route to Castel Benito (Idris) in Libya with a Senior Engineering
Officer, Air Commodore Moreshead and other staff from Transport Command Headquarters on board, a total of 9 passengers and
7 crew members, including an additional Flight Engineer plus two spare Hercules piston engines as replacements for two that
had gone unserviceable on another Hastings stranded at RAF Habbaniya in Iraq, the aircraft was approaching its All Up Weight
(AUW) of 80000lbs.with other cargo on board.
The SEO and his staff were on a visit to inspect Staging Posts and other Technical Units of the Middle and
Far East Air Forces. The events that follow are bizarre to say the least as up to this accident Bristol Hercules engines had
a habit of oil gulping with the loss of all oil through the breathing system but as each engine was dependent on oil from
its own tank, the loss of more than one engine would be considered almost unheard of as oil unlike fuel could not be transferred
from one tank to another. Most four engined aircraft were quite capable of flying on 3 engines with one propeller feathered
putting the faulty engine at rest.
At 0700hrs GMT TG613 departed Castel Benito heading towards Cyprus on the second leg of its journey to cruise
at 9000ft. At 0820hrs at a position 180 miles NNE of Castel Benito and 200 miles SE of Malta the two inner engines failed
and both propellers were feathered, a radio distress message was transmitted at 0822hrs, the captain Flight Lieutenant Wright
immediately changed course to head for Benina, Benghazi, Libya which was the next available airfield along the North African
coast. Within four minutes of the first two engines failing, number one engine port outer failed and the propeller was feathered,
there was no alternative but to ditch the aircraft in the sea as flying on one engine with a maximum AUW could not be sustained.
Whilst the crew remained in the cockpit area, the Navigator and spare Flight Engineer were ordered to the
passenger compartment to prepare for ditching, whilst the crew continued to send Mayday messages, all available fuel was jettisoned
to reduce the risk of fire and explosion. Passengers and crew all donned Mae Wests and each of the emergency exits were removed
for quick escape purposes. Within eight minutes of first having diagnosed engine trouble the aircraft impacted the water where
upon both wings and the tailplane were ripped off.
Somehow the Air Quartermaster, who was at the AQM station on the Flight Deck managed to scramble over the
freight and like the other passengers were able to exit the aircraft through the port parachute door and fuselage hatches,
whereupon the freight moved and jammed up against the door leading to the flight deck, the crew of two pilots, signaller and
flight engineer vacated the cockpit by exiting through the astrodome hatch on the top of the fuselage. The order of evacuation
was pilot, co-pilot, engineer and air signaller I understand that the Air Signaller a Flight Lieutenant Pearce was still connected
by his communication lead and somehow this had wrapped around his neck and impeded his immediate exit. Bearing in mind that
the aircraft had filled up with water almost immediately and from the time of impact to disappearing below the waves only
90 seconds had elapsed!
There are many similarities now regarding TG613 and TG579. A passenger threw a J4 dinghy that was stowed by
the main door into the sea where the passengers and crew were. Fortunately, as the wings became detached from the fuselage
the 4 wing dinghies inflated as they were designed to do and the passengers and crew made there way to these dinghies for
safe refuge. Two of the wing dinghies became unusable, one having sustained a huge rip in the floor, whilst another had a
leak from the air chamber. Three of the four wing dinghies were eventually retrieved, a roll call was organised within the
dinghies and all 16 on board were accounted for, those that had suffered cuts and bruises were attended to with emergency
medical equipment on board the dinghies.
Balers and sponges were used to remove the excess water from the dinghies and a radio transmitter was attempted
to be erected via a kite but due to wind velocity below 7 knots this was not achieved.
Two twin engined Grumman SA-16A Albatross amphibian aircraft were dispatched from the large USAF Wheelus airbase
near Tripoli in a search and rescue mission , this was the C Flight aircraft of the 7th Air Rescue Squadron. One aircraft
arrived on the horizon at 1200hrs GMT and saw the discharge not of the two star red distress flares that had been fired but
the smoke from the cartridges and flew over the dinghies, within a very short period of time this aircraft dropped a two way
portable VHF radio by parachute. Contact between the Albatross and the survivors was established and they were advised that
a destroyer HMS Barfleur had been dispatched from Malta to pick up the survivors.
The survivors were advised that the if the destroyer had not arrived by sundown , a Grumman Albatross would
alight upon the water and pick them up rather than the possibility of losing sight of the dinghies in darkness. This appeared
less likely as the swell was by this time 15-20 feet, a second Albatross arrived on the scene together with a USN Lockheed
P2V-7 Neptune and a RAF Avro Lancaster carrying five Lindholme survival canisters, these were dropped nearby, later three
of the five canisters were retrieved. Later a further Lancaster arrived on the scene with an Airborne Lifeboat but this was
not dropped as a further Albatross managed to land at 1530hrs to pick up the survivors, they all stayed on board the Albatross
until the arrival of HMS Barfleur, which was guided in by a further Lancaster discharging flares at 2200hrs when they were
transferred to the destoyer. The Albatross however could not take off until the next morning due to the huge swell, in the
meantime the destroyer stood by the Albatross overnight in case of a further emergency! The Albatross managed the extremely
hazardous lift off to return to Wheelus AFB on the morning of the 23rd July. The destroyer returned to Malta with the survivors
and arrived at 2100hrs, the survivors were all returned to RAF Lyneham by air on 25th July.
To summarise: From 9000ft to hitting the water eight minutes had elapsed, three engines had failed, the wings
and tailplane were torn off, the freight shifted blocking the crews exit to the easier escape route through the passenger
compartment, 90 seconds after impact the fuselage had disappeared below the waves. These guys were extremely lucky! In the
case of TG579 we know that the aircraft was vacated within one minute, I recall being the third person out of the parachute
door within 45 seconds and that was after I put a Mae West on!
Of the nine passenger seats on TG613 all were seats normally fitted to Avro York aircraft, when 613 impacted
the water all nine seats broke free and ended up among the freight, thankfully all were rearward facing seats which undoubtedly
saved those passengers from very serious injuries.
I havent seen the Form A1180 Official Accident Report on this incident but much of the above information was
given to me by Chris Charland to whom I am deeply indebted. If there is anyone who can throw any light on to this crash please
get in touch with me.
Technical problems:
Much information has come in regarding recycled oil that the RAF used in their aircraft engines at about this
time, it is this that has given theories to engine oil gulping where the whole of the oil capacity within the oil tank is
discharged through the engine breathers, eventually leading to no oil for lubrication purposes, friction builds up resulting
in the loss of power from that engine. I have already mentioned that there is no way that oil could be transferred from one
engine to another therefore in such circumstances that engine becomes isolated. It is known at about this time in the early
1950s that there was an ongoing problem with Bristol Hercules gulping oil, I can only recall one incident of this happening
on a Hastings aircraft and the resultant mess was apparent for all to see!
On TG613 we know that both inboard engines were isolated and the propellers feathered, it is also thought
that Number 1 engine had an overspeeding propeller and that too had to be feathered, it is also known that one Hastings crashed
as a result of an overspeeding propeller, which flew off and hit the fuselage. It is hard to believe that three engines, independent
of each other, should fail within a period of four minutes of the first such failure. Some analysts have stated that the engineering
team were on board 613 to ascertain the problems of oil gulping first hand, well if this was the resultant cause, they then
had first hand knowledge of this and ironically were the first passengers to lose at least three engines on a single leg of
a journey flying in a Hastings and ending up in the sea!
In 1953 I had just turned 14 years of age, I was mad keen on flying in whatever aircraft I could go up in,
my father Flight Sergeant Joe Cooper was stationed at RAF Lyneham and was in charge of Aircraft Servicing Flight (ASF), and
as long as I wore an Air Training Corps uniform I could fly in almost any type that wasnt leaving the shores of the UK. As
the Handley Page Hastings aircraft was the dominant transport aircraft this would be the type I would often fly in. I recall
the discussion my father had with me after TG613 crashed as it was still school holidays when my flying activities took place,
and he asked me if I still wanted to fly in those aircraft? This was not a problem to me then, I also recall how after the
Board of Inquiry had convened and the result was announced as to what caused this accident, well like all other RAF accidents
this would have been subjected to the thirty year rule applying on all aircraft crashes and I recall him saying this was as
a result of the wrong type of oil being put into the engine oil tanks at Castel Benito. As
I recall the incident at that time some local labourer at CB filled up the engine oil tanks with Oil Mineral Detergent (OMD)
this was a flushing oil used to thoroughly cleanse every working part of an internal combustion engine and was only used during
major engine servicing. Detergent oil would rid the inner workings of all of the impurities within the engine, it was a cleansing
agent and under pressure and heat would cause frothing and under prolonged use would overheat the engine and the oil would
be exuded through the breathing system. Oil Mineral was the usual oil to be used, unfortunately in my time in the RAF (1956-1969)
the oil bowsers were always painted an air force blue colour and the only difference to the two oils was shown on a white
or yellow circle with the code OM(D)270 or OM270 and this is where the confusion arose.
If the wrong oil had been inserted into say two, three or maybe all four oil tanks then the effect would all
be found at the same time, say 80 minutes after take-off from CB and all engines malfunctioning within a few minutes of each
other which in fact was the case. After my drop in the ocean at RAF Gan in 1960 my father narrated the same story to me on
my arrival home and so this has lived with me vividly for very nearly 50 years. I do not know what the Accident Report says
about this oil but this is my theory and after all if this was kept under wraps under the 30-year rule who would be about
today to dispute this theory.
Updated 9th October 2003 I have today received the Accident Report Form
A1180 as kindly supplied from the RAF Museum at Hendon. There is scant information which follows:
Pilot Flight Lieutenant J C Wright * AFC Aged 32 holder of Master Green
Instrument Rating Certificate
Co-Pilot Pilot Officer M B Geldart(? spelling) Aged 23 who according to
the 1180 had not flown a Hastings as Co-Pilot previously.
Of the 14 people on board (The information from the RCAF Archives states
16 as there was a spare Flight Engineer on board! So here there is a discrepancy):
Casualties: 6 passengers including A/Cdr Moreshead slightly inj(ured)
3 Passengers & 5 other members of crew uninjured
On the reverse of the Accident Record Card the only other wording is:
3 engines failed in flight - a/c ditched successfully - became submerged
in approx 2 mins.
412:- Cause of engines failing not established. Some items of distress organisation
criticised.
Remedial Action: Action by Command & AM (Air Ministry), taken(?) on
items in distress organisation criticised by court - See Acct(???) file
A precise location for this accident is given as 3230N 1750E
This accident report, is like all others, is handwritten and is not completely legible.
*Updated 5th November 2003, Russell Wright the son of Flight Lietenant J C Wright has made contact to inform
me that his father was awarded the Air Force Cross (AFC) in the New Years Honours Awards of 1954.
Updated 27th December 2004
Walter Cockerell forwarded this account to me regarding the SAR rescue mission:
I was a signaller on the second Lancaster from Luqa and we dropped the
Lindholm
canisters. The standard procedure at Luqa was to have one
Lancaster from 37 or 38 squadron on standby for SAR duties and
this would
be fitted with an airborne lifeboat. On this particular morning the
first aircraft to take off for the search
was the 38 squadron Lancaster
which was carrying the airborne lifeboat. As the survivors were safe in
a dinghy when
the aircraft got to their position it was decided not to drop
the lifeboat so we took off from Luqa at 1005 in TX273 'Victor'
of 38
squadron with the Lindholm gear and homed on to the first Lancaster.
When we got there we dropped the canisters,
before the amphibian
touched down. At that time the sea looked too rough for it. One of the
cords connecting the canisters
snagged on part of the aircraft and
broke and that was the reason that only three canisters were recovered.
Later
the Albatross touched down with a tremendous splash
and disappeared in the spray. Looked as though it had sunk. Then it
reappeared and taxied up to the survivors and took them on board.
Having done that it called us on VHF to say that
it was over its all up take
off weight and would have to wait for the destroyer and please tell them
not to come too
close as they didn't want to be sunk. We stayed at the
site for some time until relieved by another Lancaster and passed
the duty
destroyer on the way back to Malta. A most impressive sight at full
speed in quite a heavy sea.
I would love to hear from you if you have any comments you wish to make.
Copyright 2008 John Cooper